1275 S BLOCK PROBLEM
Posted: Tue Aug 05, 2014 7:15 pm
Sadly I have just discovered a gudgeon pin has walked out and ruined the bore in my S motor, my trouble is its already at 73.5mm. I reckon my options are;
1 Try to get it linered and then go for a reduced bore size which will probably reduce performance
2 What are the chances of going out to 74mm?
3 Try to put the bottom end into a pre A Plus block, I'm not sure if the crank will be a straight swop?
Now, I'm also wondering why the pin moved in the first place, its gone both ways actually. Press fit rods btw, so should I bin the rods too, have a midget set available here, but then will I not trash the pistons (omegas) getting them off the rods now? Or keep the existing rods and use Teflon buttons?
1 Try to get it linered and then go for a reduced bore size which will probably reduce performance
2 What are the chances of going out to 74mm?
3 Try to put the bottom end into a pre A Plus block, I'm not sure if the crank will be a straight swop?
Now, I'm also wondering why the pin moved in the first place, its gone both ways actually. Press fit rods btw, so should I bin the rods too, have a midget set available here, but then will I not trash the pistons (omegas) getting them off the rods now? Or keep the existing rods and use Teflon buttons?