Re: 1965 Morris Mini - From NZ to the UK!
Posted: Mon Aug 01, 2022 9:11 pm
Well, that was an unexpected turn of events!
I sold my 2006 JCW on Friday afternoon, so I made my way to the garage to collect the Mk1 to use as a runabout while hunting for a new daily. Of course, it decided on the way home that this would be the perfect time to lose compression on cylinder 4, spit out some coolant, and start to get a little hot...
All signs pointed to head gasket failure, so rather than risk driving the rest of the way home, I opted to wait for recovery and got it towed instead. Better safe than sorry!
I got started on Saturday morning - the bonnet was removed so I could crack on with draining fluids and unbolting various gubbins to remove the head.
Carbs were first up, I got to work disconnecting the fuel line along with the choke & throttle cables after getting the rocker cover out of the way.
I opted to remove them separately from the manifold, this proved to be much easier than trying to take the entire inlet assembly off in one go as I've done previously.
Slowly but surely, my parking space started to look like a bit of a junkyard
Once the fluids were drained, it wasn't much longer before the rocker assembly, pushrods and cylinder head were removed.
Lo and behold, suspicions were well and truly confirmed - the gasket had completely gone between cylinders 3 and 4. Oh dear!
All of the residue and gunk was cleaned up, and a new Payen BK450 gasket was fitted ready for everything to go back together. It was nice to see that the bores were in good condition with the cross hatch marks still visible, and I was also able to verify that the head was very much of the big valve variety!
Just like they say in the manuals, "refitting is simply the reverse of removal", and just like magic it's now looking like a complete engine again...
After torquing the head down and topping off the fluids with fresh oil & coolant, it fired right up and sounded lovely! It was run up to temperature and thoroughly checked for leaks, before the carbs were checked for balance and mixture. It turns out they were pretty much spot on, and I suspect that the head gasket must've been on its way out for some time before finally blowing on Friday - I've been struggling with erratic idle and part throttle driveability for a little while, but this has now been completely cured.
A good 50 miles of gentle motorway driving allowed everything to bed in, after which the head was checked and retorqued as required. A quick check of the plugs verified a good fuel mixture, and the power delivery is now lovely and smooth right through the rev range, so everything is now working as expected.
These cars sure know when to pick their moments, but thanks to some decent weather and some helpful friends offering me gasket sets and tools to borrow, it wasn't too much hassle to fix in the end. The joys of classic Mini ownership!
I sold my 2006 JCW on Friday afternoon, so I made my way to the garage to collect the Mk1 to use as a runabout while hunting for a new daily. Of course, it decided on the way home that this would be the perfect time to lose compression on cylinder 4, spit out some coolant, and start to get a little hot...
All signs pointed to head gasket failure, so rather than risk driving the rest of the way home, I opted to wait for recovery and got it towed instead. Better safe than sorry!
I got started on Saturday morning - the bonnet was removed so I could crack on with draining fluids and unbolting various gubbins to remove the head.
Carbs were first up, I got to work disconnecting the fuel line along with the choke & throttle cables after getting the rocker cover out of the way.
I opted to remove them separately from the manifold, this proved to be much easier than trying to take the entire inlet assembly off in one go as I've done previously.
Slowly but surely, my parking space started to look like a bit of a junkyard
Once the fluids were drained, it wasn't much longer before the rocker assembly, pushrods and cylinder head were removed.
Lo and behold, suspicions were well and truly confirmed - the gasket had completely gone between cylinders 3 and 4. Oh dear!
All of the residue and gunk was cleaned up, and a new Payen BK450 gasket was fitted ready for everything to go back together. It was nice to see that the bores were in good condition with the cross hatch marks still visible, and I was also able to verify that the head was very much of the big valve variety!
Just like they say in the manuals, "refitting is simply the reverse of removal", and just like magic it's now looking like a complete engine again...
After torquing the head down and topping off the fluids with fresh oil & coolant, it fired right up and sounded lovely! It was run up to temperature and thoroughly checked for leaks, before the carbs were checked for balance and mixture. It turns out they were pretty much spot on, and I suspect that the head gasket must've been on its way out for some time before finally blowing on Friday - I've been struggling with erratic idle and part throttle driveability for a little while, but this has now been completely cured.
A good 50 miles of gentle motorway driving allowed everything to bed in, after which the head was checked and retorqued as required. A quick check of the plugs verified a good fuel mixture, and the power delivery is now lovely and smooth right through the rev range, so everything is now working as expected.
These cars sure know when to pick their moments, but thanks to some decent weather and some helpful friends offering me gasket sets and tools to borrow, it wasn't too much hassle to fix in the end. The joys of classic Mini ownership!