I tried on the new wheels during the week
![Image](https://farm8.staticflickr.com/7512/15938762828_bba77323ff_b.jpg)
They are nice and wide!
![Image](https://farm8.staticflickr.com/7502/16124281591_17f0fe484c_b.jpg)
Then went out for a drive. The new wheels drive so much nicer!
Today I installed my stage one kit I got a few months ago. Here's the engine bay before I started.
![Image](https://farm8.staticflickr.com/7537/16144521925_00aaf60fd2_b.jpg)
And here's the view from the rear. There's a little exhaust pipe there somewhere!
![Image](https://farm8.staticflickr.com/7474/15958753697_d594ff38b7_b.jpg)
First up the HS2 carb and filter housing were removed
![Image](https://farm8.staticflickr.com/7580/15957217910_5e2b505a2d_b.jpg)
The cast intake/exhaust manifold was removed next
![Image](https://farm8.staticflickr.com/7554/16144702315_3930791eea_b.jpg)
I removed the entire exhaust system and put it next to the new one. It was about 30 minutes to get to this point..
![Image](https://farm8.staticflickr.com/7470/15524799023_e99a029ba2_b.jpg)
And a close up of the old and new manifolds and carbs
![Image](https://farm8.staticflickr.com/7545/15524966723_78eaeed99c_b.jpg)
So now we have the new parts going on - first on was the exhaust manifold. I had to lean the engine forward a bit to fit it in. This took about 40 minutes to get in..
![Image](https://farm8.staticflickr.com/7577/16142796171_5b51e4d4d3_b.jpg)
Intake manifold was next.. I had to grind a flat edge on the two inside washers as I couldn't get them to sit flat. I put the new studs in too
![Image](https://farm8.staticflickr.com/7538/16143992232_1603f8ce97_b.jpg)
The HS4 took about an hour to get installed... I had to borrow some bits from my other carbs and that took a bit of time to get sorted. The new AAC needle went in fine. The old one was an ADF.
![Image](https://farm9.staticflickr.com/8648/16144755185_a104c721f2_b.jpg)
The KN filter was installed in the filter housing
![Image](https://farm8.staticflickr.com/7519/16144001272_be158e136a_b.jpg)
Everything is mostly done in the engine bay in this photo. I've got to get another choke cable as mine was too short to reach, as its on the opposite side to the old HS2
![Image](https://farm8.staticflickr.com/7487/16118975326_a5f327b4bd_b.jpg)
I got the RC40 twin box exhaust installed easily and went to connect the battery back up again, which resulted in some big sparks! It took me a while to figure out what the deal was, but it turned out the new exhaust was touching the floor starter button! I tried moving the exhaust to miss the button but soon came up with a good fix..
![Image](https://farm8.staticflickr.com/7485/16144478595_ff6ee385e8_b.jpg)
It was all good once fitted!
![Image](https://farm8.staticflickr.com/7477/16143720082_e01c96bc2d_b.jpg)
You can actually see the exhaust from the back now!
![Image](https://farm8.staticflickr.com/7567/15525038683_d2c4305751_b.jpg)
It fired up first time, which was awesome! I had to up the idle speed a bit to get it stable and idling nicely. I set the mixture a bit richer and took it out for a quick drive. I didn't really need the choke to get it going as it was 30 degrees today! It's got noticeably more grunt now, which is great, but it's not too much louder from the inside, which is slightly disappointing... There is a lot more intake noise though!
I've still got to fine tune a few things, and give it another oil change...